C2762 - Pacific Wire Ltd - Wire Manufacturers
- Auckland Region
Summary
The total annual savings resulting from CP options implemented to date are
estimated as well over $0.5 million per year with a payback period for each
option implemented varying from immediate to less than one year. The adjustment
of the raking procedure alone saved the company several $100,000s per year
and increased product throughput.
Business Profile
Pacific Wire manufactures galvanised and bright wire for various applications
such as fencing, nails, steel mesh, armoured wire for cables. Processes include
the mechanical drawing of wire from steel rods, wire cleaning and galvanising.
The company employs 80 staff.
Type of Project
Cardboard and paper recycling, boiler shutdown during non-production hours,
installation of a central power switch and daylight sensors, reuse of steam
condensate from cleaning baths, recovery of bath dragout, regeneration of
sulphuric acid, caustic soda regeneration, and raking adjustment to prevent
lumps on wires.
Reasons for Project
Waste reduction is part of an operational excellence (OPEX) programme. OPEX
is Pacific Wire's continual improvement programme which has an objective
of enhancing operational effectiveness through energy savings and minimising
waste to bring benefit to the company. Management are also committed to producing
products in an environmentally responsible way.
The Project
Cardboard and paper recycling
| Details |
Since September
1996 Pacific Wire has segregated cardboard and paper for
recycling. Approximately 85 kg of loose office waste paper
is collected per month or 1 tonne per year. Approximately
25 kg of cardboard is collected per month or 300 kg per year. |
| Economics |
Cardboard collection costs $5/month bin rental and $7.50
per bin pickup = $150/year.
Paper collection costs are $2.50/week per bin for 8 bins
and no costs for pickup = $960/year. Bin purchase will
eliminate rental costs and is being investigated.
Savings include reduced disposal costs of $90 per year
($69/tonne) and reduced pickup costs of $600 per year ($50
per monthly pickup). Annual costs for recycling are therefore
$270, but will quickly become savings when bins are purchased.
|
| Benefits |
Reduced paper and
cardboard waste of 1.3 tonne per year. |
Boiler shutdown during non-production hours
| Details |
The production hours
at Pacific Wire are 120 hours/week or 5 continuous days.
Previously the boiler operated for 142 hours/week. The boiler
is now shut down during weekends and now operates 128 hours/week
(the 8 hour additional hours are required to start up the
boiler before production begins on Monday mornings). As a
result, gas for heat the water, electricity for the water
circulation pump, and chemicals used to reduce water hardness
have been reduced. |
| Economics |
Gas savings are
$ 4800 per year. The payback period is immediate. |
| Benefits |
Reduced gas, electricity
and chemical consumption and costs. |
METAL CLEANING PROCESS
Reuse steam condensate for cleaning baths
| Details |
Steam condensate
from heated borax and metasilicate tanks is collected and
used to fill and heat the rinsing tank. Approximately 5.4
m3 water per day or 1,971 m3 per year is saved. Also, 144,000
kWh is saved per year because the rinsing tank requires less
heating. The condensate was collected from the steam traps
and was transported into the tanks. The work undertaken by
maintenance staff to install hot water recycle pipelines
and material costs were nominal. |
| Economics |
Water savings are
$1,080 per year and energy savings are approximately $3,000
per year. The payback period is immediate. |
| Benefits |
Reduced water and
energy consumption and costs. |
Recovery of bath dragout
| Details |
Pacific Wire have
a series of five cleaning tanks. Rubber sheets were placed
between the different cleaning tanks to prevent dragout spillages
caused by moving objects from one tank into the next. As
a result, chemical consumption and trade waste discharges
were reduced. |
| Economics |
Six rubber sheets
cost $360 ($60 each). Savings have not been determined. |
| Benefits |
Reduced chemical
consumption, including acids and sulphates. Reduced wastewater
stream. |
Regeneration of sulphuric acid
| Details |
The
first stage of making wire is the pickling of the rod steel.
This is
done in pickling baths of dilute sulphuric acid which removes
rod scales, rust and dirt. The acid requires replacement
when the iron level reaches 12%. Use acid from the pickling
baths is recycled by an acid recovery process (see diagram).
The liquid is cooled to 0°C where iron salts crystallise
and precipitates to the bottom of the cooling tank. The weak
acid which is free of iron is syphoned back to the pickling
tank for reuse. The crystals are removed via draining bins
into hoppers. They are then sold as "ferrous sulphate heptahydrate" (ferrosulphate)
for fertiliser blending. Each year approximately 4,000 tonnes
of diluted (= 200 tonnes of undiluted) sulphuric acid is
recycled and approximately 500 tonnes of ferrosulphate is
produced for sale. |
| Economics |
The existing system
is overhauled which costs $50,000. Annual savings are $231,000
including: - $126,000 ($630/tonne) from reduced sulphuric
acid consumption; - $50,000 ($100/tonne) from ferrosulphate
revenue; - $55,000 reduced trade waste costs through reduced
disposal of spent sulphuric acid. |
| Benefits |
Reduced wastewater
stream, sulphuric acid consumption and associated costs.
Income from selling ferrosulphate as fertiliser. |
Caustic soda regeneration
| Details |
Caustic soda is used in one of the cleaning tanks and
becomes contaminated with boron from the previous cleaning
tank. By cooling the caustic soda, the contaminants form
a gel which is subsequently separated from the weak caustic
soda solution by filtration in a filter bag. Following
treatment the gel is landfilled. The clean caustic soda
is reused in the cleaning tank. Each year 20,000 L of caustic
soda is recycled rather than discharged into the sewer.
Water consumption has also been reduced by approximately
300 m3/year.
|
| Economics |
The system cost
$17,000 to install and $18,000 a year to operate. Total savings
are $56,000 and include: - reduced caustic soda consumption
of 20,000 L per year - reduced disposal of caustic soda solution
of 46,000 per year - reduced trade waste costs associated
with caustic soda disposal. - reduced water costs of $192
per year. The payback period is 6 months. |
| Benefits |
Reduced caustic
soda consumption, disposal and costs. Reduced water consumption
and costs. |
METAL FINISHING PROCESSES
Raking adjustment to prevent lumps on wires
| Details |
Following the galvanising
process, hot zinc wires are passed through gravel to remove
any zinc dross formed during the process of galvanising.
Employees use a stick or rake to loosen the gravel, but where
they touch the wires lumps are formed which need to be cut
out losing valuable product and labour time. A modified tool
was made and employees were instructed how to rake the gravel
without touching the wires. Wire waste was reduced by 1,000
kg per day or 300 tonnes per year. |
| Economics |
No costs were involved
in modifying the rake. Savings through reduced raw material
consumption have not been fully costed but are estimated
as several $100,000s per year. The payback period was immediate. |
| Benefits |
Reduced zinc dross
and production loss estimated at several $100,000/year. Improved
product quality. Increased productivity through increased
throughout as fewer stoppages. |
For additional information contact:
Shiu Singh,
Pacific Wire Ltd,
PO Box 22198,
Otahuhu,
Auckland
Ph 09-2704249
Fax 09-276576
For further information about Cleaner Production in the Metal
Industry see:
Opus International Consultants (September 1997): Cleaner
Production Guide for the Metal Industry- Minimising waste,
reducing costs and caring for the environment.
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